To briefly describe the roaster, it is provided with a small, fan-speed-control PCB that has a knob attached to it to control the fan speed. The circuit is designed to ensure a minimum operating voltage of 4 volts for the DC motor of the fan, and a maximum operating voltage of 13.5 volts. This minimum bound on the fan speed/voltage is intended to secure the heating element from being damaged, or from damaging the surrounding wires and electronics. The DC voltage is provided to the DC motor using a laptop's switching power supply (a.k.a. charger). This type of power supplies is different from a conventional transformer in the sense that it's very efficient and automatic with regard to the input voltage (i.e. will always produce a regulated 15.5 volts regardless of the input AC voltage). The fact that I used this type of power supplies for the fan control circuit means that the whole roaster can still be operated using a Variac with only the heating circuit being effected by the varying input AC voltage.
That is for the fan circuit. For the heater circuit, on the other hand, I used a 220V/1000W dimmer switch (made in China, sold for 35 S.R. -less than $10). I pulled the dimmer circuit out of its casing, attached a small heat sink to the back of the output transistor (the electronic component that dissipates most of the power), and added a small 12V cooling fan to the side to aid in its cooling. This active cooling of the cheap 1000W dimmer seems to allow me to use this dimmer to control the 220V/5A heating element without damage. I also used a panel current meter to watch the current being passed to the heating element, since the relationship provided by the dimmer switch is highly non-linear. Note that in the case of the fan control circuit, the circuit is highly linear by design (half way = half power), and thus needs no such addition.
The modification didn't cost much in total if we only calculated the cost of the parts that made it into the roaster, but it was very tedious. Note that one of the most expensive parts was already available, which the the 15.5V/5A TOSHIBA laptop charger. I bought a replacement charger 3 years back for my laptop when the original charger stopped working due to a mechanical shock. I was fortunate enough to examined the old charger today to figure out that one of the inductors was broken off the board, and by only soldiering the inductor back to its correct place on the PCB, the charger was working again.
I said that I was going to describe the roaster in brief but I seem to have given an exhaustive explanation of it, which I think is good thing.

It's generally not a good idea to work on the mechanical and the electronic aspects at once, it can lead into a big mess in my opinion.

From the fan motor back (clockwise in circular fashion): the simple fan control circuit with a heat sink attached to it, the original heating chamber of the pop-corn popper, the heating element assembly (to be put inside the heating chamber), the 15.5V switching power supply (a.k.a. laptop charger), the 10A panel current meter I bought (50 S.R.), and finally, the small 12VDC cooling fan I bought (10 S.R.).

Extremely tired...


The inside of the roaster is very crowded. I don't believe we were able to put everything inside. Note the (out-of-focus) Aluminium tube spacer we used to clear some space at the bottom, this lead to increasing the height of the roaster and not being able to put the lid on in its place, but had the great advantages of allowing us to put everything inside and making the electronics far from the heat of the chamber.

The solution I used to solve the height problem, note that the springs were ideal since they were in balance with the push-away spring attached to the heating assembly, which in turn prevents the assembly from touching the roasting chamber (if you don't get this, it's not an important detail).

Without the lid, springs still on.


The very first roast, hard bean, not well dried, not well developed, chlorine-pool tastes, etc.

In action, not enough light for photography.

The panel current meter, it has 10A written on it but in actuality it shows up to 20A. Note that for this roaster I only use the range from 0A to 5A.

The electronics cooling fan. You may think this is a little bit over-engineered but I think the electronics needs it. I know that the roaster fan already provides enough airflow to cool the electronics but I wanted to be sure... The fan is positioned to cool the side of the dimmer which contains the power transistor.

The switching power supply did not fit wholly inside so I had to add this extension, which is cut from the plastic of the charger casing. Note that the cable of the machine can now be plugged and unplugged.

We also moved the power switch to become closer to the knobs.

The upper knob is for the fan, whereas the lower knob is for the dimmer (i.e. the heating element).
I am very happy that I finally succeeded in modifying a popper, which I think will make me delay the QUEST M3 roaster purchase I already discussed in this forum. It's always better to be exposed more to something similar to the thing you want to buy.
































